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       #Post#: 35851--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: Stoker Date: February 17, 2021, 3:38 pm
       ---------------------------------------------------------
       If it was just smeared on the valve linkage rod as shown in that
       prior photo, it would have been no problemo! However .... that
       stuff was fully packed in under the packing gland compression
       cap nut, and all along inside of the rod guide tunnel, so there
       was in fact a substantial amount of the gunk to be dug out from
       inner recesses.
       It was pure joy to be sure!!!
       Do note in that same photo, there are only just barely a full 5
       threads on the end of that rod, and they are pretty chewed up,
       which doesn't make for a very firm grip or solid alignment, nor
       does it allow for much adjustment. The clevis head that screws
       on there only had four threads in it, so couldn't even go on
       that far, even though it had an I.D. depth capable of taking a
       full 10+ threads with a bottom tap. So I did go ahead and tap it
       to full depth, and took a die to the rod and gave it a full 14+
       threads so that I could also mount a jam nut to lock off the
       clevis position!
       [attachimg=1]
       [attachimg=2]
       Yes ...  that hole is not very well centered either, but at
       least there is plenty of "meat" around it!
       #Post#: 35852--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: classixs Date: February 17, 2021, 3:52 pm
       ---------------------------------------------------------
       Thanks for sharing the good and bad details here Daniel, and
       well done on getting that clevis head properly fixed to the rod.
       Do you intend to eventually fix the misaligned holes as well?
       #Post#: 35855--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: Stoker Date: February 17, 2021, 4:13 pm
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       [quote author=classixs link=topic=3787.msg35852#msg35852
       date=1613598757]
       Thanks for sharing the good and bad details here Daniel, and
       well done on getting that clevis head properly fixed to the rod.
       Do you intend to eventually fix the misaligned holes as well?
       [/quote]
       Probably not Jan ... at least not at this point. There is so
       much that could be done, but for now I'll just concentrate on
       what must be done to get this big boy up and running at some
       reasonable level. Perhaps then I can go back through it and fix
       some of the more egregious issues that don't necessarily impact
       its ability to function.
       I originally suggested, back before I made the drive to get it,
       that what I was buying was just a "pig in a poke", and that is
       exactly what it turns out that I got. I'm actually far ahead of
       what my postings here show, so I know full well at this point
       what the big picture is, and it isn't any too pretty. Still, I
       have faith that it can yet be turned into a decent runner as
       most of the key machining was likely done by the factory, so it
       is just the ancillary work that has problems .... for the most
       part anyway.
       In the end, this engine should prove fully capable of all that I
       will ever ask of it, which won't be much, as I don't have much
       in the way of providing it with the steam, or even air power,
       that it truly needs to work properly. I do believe, now that I
       really know what I have, that I will be happy with this engine,
       even with all of its obvious problems and poor machining, if for
       no other reason than I would never likely have parted with the
       money that an truly good 1/2 hp Sipp should properly bring!
       Hey ... if nothing else .... it has a nice paint job!?!?
       #Post#: 35863--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: Jim Date: February 17, 2021, 5:08 pm
       ---------------------------------------------------------
       Thanks for the pics and the update Daniel.
       #Post#: 36117--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: Stoker Date: February 20, 2021, 8:52 pm
       ---------------------------------------------------------
       All righty then kids .... back to this ongoing mechanical
       adventure, and sorry for the extended delay. Likely to be more
       of the same before this tale of woe is complete, but no hurry
       anyway as it isn't going anywhere under its own power anytime
       soon!
       So last post I was inside the steam chest, and while I found the
       D-valve and port face to be fairly flat, albeit with somewhat
       rounded edges and corners, and not entirely smooth, I decided
       that I'd do a bit of lapping and also try to clean up and square
       the ports themselves which were a bit out of square with some
       wildly irregular edges. Turns out that took a fair amount of
       time as the casting inside the port channels was pretty rough,
       and even though I didn't do a true clean-up of all of that, I do
       believe the steam flow will now be somewhat enhanced and the
       cut-off should be a bit crisper as well, however I was unable to
       truly "square" the port edges, and they actually seem to slant
       slightly to the motion of the valve. Perhaps they are supposed
       to as a means of phasing the open and closing of the port?
       Probably not, and it is just another weird artifact of a poor
       build, though this one does seem to be cast in and nearly
       irremediable. Should run better now in any event!
       [attachimg=1]
       [attachimg=2]
       There is also a noticeable casting flaw in both the D-valve and
       port face surfaces that would take really serious lapping, or
       even milling to get past, as would the rounded edges and corners
       on both faces. For now I'll not go that far,and likely never
       will, but it could be an option if it turns out to be necessary.
       I should add that the other end of the valve linkage seems
       pretty okay just the way it is. The eccentric seems reasonably
       well made and fitted with shims that will allow for adjustment
       with wear. Although the linkage rod is "S" bent, and it likely
       wouldn't have to be if the eccentric cam had been put on the
       other way around, there really isn't any problem with it done
       this way, and I have now seen photos of at least a few others
       done this way as well.
       #Post#: 36122--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: Jim Date: February 20, 2021, 10:00 pm
       ---------------------------------------------------------
       Thanks for the pictorial update Daniel.
       #Post#: 36127--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: St Paul Steam Date: February 20, 2021, 10:13 pm
       ---------------------------------------------------------
       Yes , thanks for the update , following along closely here .
       #Post#: 36159--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: tenniV11 Date: February 21, 2021, 12:12 pm
       ---------------------------------------------------------
       Thanks for the story - the tuning will be closely overviewed
       perfect the lapping...
       Arnold ;D
       #Post#: 36183--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: classixs Date: February 21, 2021, 4:20 pm
       ---------------------------------------------------------
       [quote author=St Paul Steam link=topic=3787.msg36127#msg36127
       date=1613880835]
       Yes , thanks for the update , following along closely here .
       [/quote]
       Ditto  :)
       #Post#: 36215--------------------------------------------------
       Re: Bargain 1/2 hp G. Sipp .... the good, the bad & the ugly
       By: Stoker Date: February 21, 2021, 6:34 pm
       ---------------------------------------------------------
       Let's call it a day on the valve linkage / steam chest side of
       this beast, and head back up to the flywheel / crankshaft
       assembly. With the valve linkage fully disconnected, the
       noticeable bind in flywheel rotation was still present. So my
       next move was to disconnect the crank rod from the crank and see
       how that might be affecting rotation.
       Sure enough, rotation smoothed out almost completely with only a
       slight and fairly even resistance felt through 360 degrees of
       rotation. Whew!
       With just a very slight loosening of the cap screws holding the
       bearing clamps in place, the flywheel spun easily through
       several rotations coming to a slow and even stop that bodes well
       for the shaft and bearings I think. With the bearing clamps in
       this ever so slightly loosened condition I tried to wiggle the
       crankshaft and felt no noticeable movement. This seems real good
       ... perhaps too good to be true?
       Along the way, I thought I'd take the time to check for any bend
       in the crankshaft, with the shaft still cradled in its bearings.
       So I got out an indicator set-up and with the tip set as close
       to the hub of the flywheel as I could manage, took a set of
       rotational readings that gave me less than .002" runout, and
       some of that could easily be due to old varnished oil, though
       probably not.
       [attachimg=1]
       In any event, it is now apparent that the drag/bind issue was
       going to be found in the piston/cylinder/crosshead-slide/
       linkage system, and not with the crankshaft or bearings .....
       again, WHEW!!!
       I should add that perhaps surprisingly, the connecting rod's
       holes at both ends seem fairly well centered, though not
       perfectly, and both the crosshead-slide and crank arm holes
       while not too well centered, are both adequately so, as to have
       plenty of "meat" around them, and should offer no problems. The
       crank end of the connecting rod has a set of brass bearing
       inserts that will need some adjustment as there is a little slop
       on the crank arm bolt (crank pin), and the adjusting screw for
       that bearing set cannot further tighten, so the edges where the
       two bearing halves meet will need to be filed back ever so
       slightly to allow further adjustment range.
       [attachimg=2]
       [attachimg=3]
       [attachimg=4]
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