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       #Post#: 40518--------------------------------------------------
       Back to the Beast .... Big Sipp Problems
       By: Stoker Date: April 18, 2021, 4:34 pm
       ---------------------------------------------------------
       Just thought that as I'm sort of taking the day off, I'd go back
       in time six weeks or so and continue the saga of problems found
       on this "Bargain" half horse Sipp.
       After finding that the crankshaft was not causing the bind, it
       was time to disassemble the piston rod, crosshead and open up
       the cylinder to find where the bind actually was coming from. As
       noted before, the crank rod ends seem not the issue either, and
       to further examine that linkage train, I will now note that the
       crosshead slide seems to have just about the right amount of
       "slop" or tolerance, to slide smoothly without binding, though
       the slide shoes are shimmed with gasket material to attain a
       closer tolerances for that clearance.
       [attachimg=1]
       Having disconnected that from the piston rod, next move was to
       open up the cylinder end cap, free the piston rod packing gland
       nut and back the piston out of the cylinder. While this was
       easily done, as it appears there was only a sleeve in the
       packing gland and no actual packing, it was noticed that there
       was more than a little drag on the movement of the piston as it
       was pushed back in the cylinder. So it seems that at least a
       goodly part of the rotational drag noted on the flywheel/crank
       assembly likely has the piston/cylinder as its source, so much
       further investigation was needed here next!
       Upon opening up the cylinder and removing the piston, a couple
       of other telltale features were immediately noted. First, the
       cylinder cover bolt hole drilled and tapped just above three
       o'clock violates the steam passage port from the steam chest,
       while the next one down at about five o'clock into the rim of
       the cylinder, had initially been miss-located, but was caught
       and corrected before it had been drilled too far, or more likely
       the pre-assigned spot was missed to match with a misalignment in
       the drill holes of the cylinder end cap. Whichever is the case,
       something wasn't done quite right, as seen here:
       [attachimg=2]
       Also note in this photo, at the front end of the cylinder
       (rather out of focus) the drill gouge and threading marks from
       the large hole that was drilled and plugged into the front
       bottom of the cylinder for no known reason.
       But an interesting aspect of this is that while that hole and
       plug are down at about seven o'clock in the photo, the gouge and
       thread marks are up at around ten o'clock, so that brass front
       face of the cylinder is an insert that is pressed of screwed
       into the cast iron cylinder casting, in order to provide for the
       piston rod packing gland set-up as seen here:
       [attachimg=3]
       Now, even at this point I'm unsure as to whether this brass
       packing gland assembly "insert" is just pressed in or actually
       threaded, but I suspect it is only an interference press fit,
       and will test this assumption the next time I tear the engine
       down. Based on the rotation of the plate on the inside of the
       cylinder, as evidenced by the changed location of the drill
       gouge, it could be either, but a press fit perhaps makes more
       sense, we shall see.
       In any event, now knowing at least much of the drag is coming
       from the piston/cylinder combo, I felt it time to make do a
       little measuring, testing and hopefully improving any situations
       that were remedial in this area. Thus I measured the cylinder
       bore for cylindrical conformity in a couple of different ways:
       [attachimg=4]
       [attachimg=5]
       Having so measured the bore all around and in and out, I found
       it to be quite consistent within a couple of thousands, and
       believe that runout only to be caused by the roughness of the
       bore, due to a scale or corrosion build up mostly along the
       bottom 1/4 where you'd expect condensate to collect after a run.
       It seems likely the cylinder was originally factory bored to be
       this good compared to how much of the rest of the machining
       seems to be done. To be sure the worst of the roughness was
       along that bottom portion of the cylinder, but in fact all walls
       of the cylinder seemed to be unnaturally dark with some form of
       deposit or buildup, and thus I felt the next step to take of
       benefit, would be a bit of honing of the bore. So a lashed the
       engine in an end up position to the trailer hitch ball on my
       trucks bumper, so as to align the cylinder vertically for ease
       of working, and thus reducing any tendency of gravity to cause
       uneven honing around the bore, as seen here:
       [attachimg=6]
       [attachimg=7]
       [attachimg=8]
       In the last photo you can better see (now in focus) the gouge in
       the front plate of the cylinder left over from drilling the plug
       hole that can barely be seen at about seven o'clock, and how it
       is now rotated up to about ten o'clock. This few minutes of
       honing evened the bore noticeably and smoothed it to the touch
       as well. Perhaps I'll go another round of honing next time I
       have it apart, but the upshot is that clearly doing this did
       help materially in smoothing the engines motion.
       #Post#: 40525--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: Stoker Date: April 18, 2021, 6:08 pm
       ---------------------------------------------------------
       Moving on to the piston now, there is lots to see and do here.
       First thing I noticed here was that the piston had to be made in
       at least two parts (possibly as many as four) that  were screwed
       together in order to capture the large cast iron piston ring.
       Next thing I noticed was how incredibly rough the outside edges
       of the piston face plates appeared, as seen here:
       [attachimg=1]
       Sadly, I was unable to get any kind of a purchase on the rims of
       the piston's face plates without causing damage, in order to try
       unscrewing them. Will likely make a clamping fixture to grip one
       side while I chuck the other side and may be able to unscrew it
       that way, the next time I have this engine apart, as there is
       plenty else that needs be done here, as there is much else
       wrong.
       I did feel that since I was going to reassemble the engine right
       away to try and run it a little at the GPU, that I should "clean
       up" the rough edges around the rims of the piston's face plates
       and proceeded to do so chucked up in the lathe with a collet on
       the piston rod. However, as soon as I saw the amount of runout
       both in circumference, as well as laterally, I knew that
       something was definitely not right here, so proceeded to
       indicate off of the offending surfaces and found over .007"
       difference in the two face plate's circumferences and
       concentricities, but even more staggering was that there was
       some .040" of lateral runout. Which is to say that the faces of
       the plates were wobbling wildly, the meaning of which is simply
       explained by the fact that the hole, which was drilled and
       tapped through the piston assembly to mount it on the piston
       rod, was neither centered nor square with the surfaces of the
       piston's face plates! That much lateral runout means that the
       piston sits in the bore of the cylinder at an angle about 1 1/2
       degrees off of a true 90 degrees. NOT GOOD!
       [attachimg=2]
       [attachimg=3]
       As it appeared that the piston ring was still wearing quite
       evenly, and no significant amount of running was expected soon,
       other than a short run for the GPU, I decided to defer any
       serious work on the piston problem until the next disassembly,
       when I can make a tool to take the piston itself apart, to
       perhaps rebore and retap and make an adapter insert, or possibly
       just to build a new piston. But that's for later.
       #Post#: 40529--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: Jim Date: April 18, 2021, 6:50 pm
       ---------------------------------------------------------
       Well you've certainly got a tiger by the tail with this engine
       Daniel.
       One consolation is that currently as a static model...at least
       it looks good!
       #Post#: 40536--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: Stoker Date: April 19, 2021, 12:03 am
       ---------------------------------------------------------
       Now to jump from the piston/cylinder end back down to the
       flywheel/crankshaft to hopefully wrap this tale of woe up until
       actual restorations get underway.
       Upon opening up the crankshaft bearing caps, I was immediately
       presented with a host of odd shaped and multi-layered oily
       gasket and brass shims on both sides and top.
       [attachimg=1]
       While it all seems to work okay, I think it may be wise to try
       to make a new set of shims that allow for only one in each
       position, and possibly even mill the bearing blocks themselves
       slightly to reduce the total thickness of shims required. But at
       this point all I did was to punch stamp each of the bearing
       halves, so as to assure that they would remain in proper pairs
       and properly oriented.
       [attachimg=2]
       Next to be considered was the attachments of the crank arm and
       flywheel, where a very ugly situation was discovered, in that
       there is no keyway milled into the crankshaft for the attachment
       of either of these features, which appear to be gripped by more
       of an undersized key caming action, than by anything else.
       [attachimg=3]
       [attachimg=4]
       So clearly when I do manage to get the flywheel and crank arm
       off of the crankshaft, I will be wanting to mill a keyway into
       the shaft of a size to properly accept a whole key to secure
       these critical features.
       And finally .... now onto the truly "Fatal Flaw", that makes
       this engine essentially irredeemable ...
       [attachimg=5]
       To wit, three of the adjacent spokes exhibit hairline cracks
       showing through the paint, which likely suggests that these
       spokes are in fact cracked all the way through from some former
       drop, or sideways blow to the flywheel. This is likely the
       source of the flywheel wobble noted in my earlier posting, and I
       can think of no practical way of making such a repair, so if any
       of you out there know the whereabouts of any spare half horse
       Sipp flywheels, I'd sure like to hear about it!!!
       #Post#: 40539--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: Scorpion2nz Date: April 19, 2021, 1:40 am
       ---------------------------------------------------------
       All i can say is it looks  like an interesting project .
       I would build a new piston .
       I would do some serious investigation of the flywheel does it
       wobble from the cracks or is the bore wonky
       #Post#: 40540--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: classixs Date: April 19, 2021, 3:16 am
       ---------------------------------------------------------
       Quite a few flaws of significant importance there.
       I agree with Dennis, forget about that piston, and make it a new
       one.
       In fact i think i just would have made it a fast one, running a
       teflonring or similar, just to see how the engine behaves with
       something properly sized in there.
       When the bore is properly honed, there might not even be a
       reason for anything more in your case, as it would last decades
       if merely intended to be a demonstrator, rather than an all day
       workhorse under load.
       Would be a good thing to get those bearing machined to fit a
       single shim, and the flywheel will tell whether it really is
       bent, or the bore crooked, as soon as you get it off there to
       attend the keyway on the shaft anyway.
       If it isnīt too badly bent, those 3 cracked spokes could be
       brazed, and it would be back to a relatively high structural
       health.
       #Post#: 40566--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: Gregowen Date: April 19, 2021, 9:15 pm
       ---------------------------------------------------------
       This is really a fascinating account of the many things that
       can be wrong with an old engine, and possible solutions, very
       educational, Thanks!
       #Post#: 40573--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: Stoker Date: April 20, 2021, 9:10 am
       ---------------------------------------------------------
       [quote author=Gregowen link=topic=4257.msg40566#msg40566
       date=1618884947]
       This is really a fascinating account of the many things that
       can be wrong with an old engine, and possible solutions, very
       educational, Thanks!
       [/quote]
       Thank you Sir for the kind words. Yes, very many things wrong
       with this poor beast, but time will tell if I am able to
       resuscitate it in any meaningful way.
       Meanwhile, as I'm unsure if you've gotten the WHOLE story,
       thought I'd add a couple of links here, to take you back to
       earlier related threads that provide more detail and perhaps a
       bit of insight.
 (HTM) https://www.officeofsteamforum.com/general-discussion/12-hp-g-sipp-in-the-bag/
 (HTM) https://www.officeofsteamforum.com/restorations/bargain-12-hp-g-sipp-the-good-the-bad-the-ugly/
       If you haven't already seen these .... I hope you do enjoy them!
       #Post#: 40593--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: St Paul Steam Date: April 20, 2021, 8:27 pm
       ---------------------------------------------------------
       I admire your sticktoitness re:this beast Daniel , you were
       Leary of it from the Start & rightly so , this one appears it
       will never be completely sound with anything less than a
       complete remake  but sometimes we can get it to as good as
       possible with what we have to work with . carry on good Sir . &
       thanks for the updates.
       #Post#: 40613--------------------------------------------------
       Re: Back to the Beast .... Big Sipp Problems
       By: txlabman Date: April 21, 2021, 6:38 am
       ---------------------------------------------------------
       Thanks for the detailed diagnosis of the issues with this engine
       Daniel.
       Way beyond my skills.
       The flywheel cracks are the most concerning.
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